The F-35: What Will Happen While Exploring ‘High Angle-of-Attack’, Part 3
F-18 E/F: Heritage F-18 All Fixed, But….Surprise!
Part 3 in a series of posts where we document The ‘Profound Truth’ of High Angle-of-Attack (AoA) flight testing of high performance aircraft.
The Profound Truth?
Discovery and rectification of undesirable aircraft behaviors during High Angle-of-Attack testing of High Performance Aircraft is not only the ‘Norm’, but those behaviors needing rectification/mitigation are usually complex, sometimes bizarre, and often ‘spectacular’.
As in the F-18A-D post, we will avoid mentioning all other problems that the F-18E/F program dealt with that did not have to do with the AoA performance, behaviors and testing. They still would be helpful highlighting in yet another way: illustrating how the F-35 program isn’t as ‘concurrent’ as some would lead us to believe. But I’ll (again) resist the temptation to beat that ‘dead horse’.
The F-18E/F is ANOTHER excellent exhibit of the Profound Truth.
In closing Part 2, I observed that “many of the design objectives behind the F-18E/F were focused on eliminating the extant problems and limitations of the Heritage Hornets”. In Part 3, we will observe how an entirely new set of challenges emerged for the F-18E/F. I would call the challenges “problems” if we were all thinking like Engineers: “A problem is normal, something to be expected, and something to be solved”. But too many people seem to think a problem is a reason to NOT do something (as if there is such a thing as a ‘problem-free’ path in any worthwhile endeavor). On the topic of solving problems, engineers in any field know that it is almost always the case that a feasible solution will involve making ‘tradeoffs’. The F-18E/F, like the Heritage Hornet, was no exception to the rule.
First, the specific design goals of the F-18E/F were:
1. Enhanced departure resistance and post departure (should it still occur) elimination of “falling leaf” or unrecoverable spin modes.
2. Requiring the aircraft to meet all flying quality requirements with a centerline fuel tank since this is a common operational configuration in all services, foreign and domestic.
3. Elimination of high AOA hang up and the accompanying AOA/cg restrictions.
4. The aircraft must be able to land on an aircraft carrier following most flight control failures.
5. Improved roll performance at elevated AOAs in the gear up/flaps Auto configuration.
6. Expanded tactical utility with large lateral store weight asymmetries (since high value stores are frequently deployed one at a time and can result in significant lateral weight asymmetries and aircraft maneuvering limitations after release of one store).
7. Reduction of likelihood of encountering pilot induced oscillation/aircraft-pilot coupling tendencies.
8. Adequate control following a dynamic and/or static loss of one engine (which sized the F/A-18E/F vertical tail).
9. No reduction in flight envelope for the two seat F model over the single seat E-model, since both aircraft would be mission capable aircraft. (Source: Hanley, Et Al, p. 32-6)
The F-18E/F program objectives Hanley describes were rather admirably met in the end, but Hanley also cogently summarizes the REALLY big surprise that the F-18E/F designers had to overcome.
Every flight test program encounters some “unknown unknown, “things that were not planned, thought of, or considered possible to occur in flight-testing. The Super Hornet was no exception. Early in the flight test EMD program, the aircraft experienced uncommanded “wing drop” during wind up turns and straight and level accelerations. As the program matured and the envelope expanded, it became clear that this was a serious problem that would impact aircraft performance if not corrected.
Over an eight-month period from August 1997 through March 1998, maximum resources were brought to bear to solve this problem. In all, over 10,000 wind up turns were executed on over 100 wing configurations before a solution was found. This effort required use of up to 4 of the 7 flight test aircraft to solve, causing significant rework to an already tight EMD schedule. The “wing drop” phenomenon was a rapid, uncommanded bank angle change of up to 180 degrees (if left unchecked by the pilot) that would cause a pilot to lose a guns-tracking solution on a threat aircraft. Wing drop occurred at all altitudes and from about 0.55 Mach to approximately 0.95 Mach. Extensive wind tunnel, simulation and CFD testing and analysis was conducted coincident with the flight-testing. (Hanley Et Al, p. 32-8)
I’m told that the total time to ‘fix’ the problem was close to 3 years. The Hanley paper doesn’t quite get into the root cause, and the authors’ explanation of the “fix” is really a list of corrective actions progressively tried and applied:
Some of the flight test “fixes” assessed included modified snag locations, vortex generators, grit, stall strips, modified flap scheduling, control surface biasing, fences and porous wing fold fairing covers. Eventually, the porous wing fold cover proved to be the most effective solution to the “wing drop” phenomenon, by dissipating adverse pressure gradients fore and aft of the shock forming on the wing and reducing the effect of the asymmetric stall.
There was an interim step to arrive at the ‘porous cover’ solution, whereby enterprising Navy types tried removing the wing-fold cover entirely, finding it pretty much fixed the ‘wing drop’ but created too much drag to meet other requirements. That’s when NASA stepped in with the half-way between 'none and one' cover, to make it a 'porou's cover. What the Hanley paper doesn’t really highlight at all is that the two factors that made this behavior SO alarming were 1) the abruptness of the phenomenon and 2) the apparent randomness of the direction the plane would roll.
What was it that happened between the Heritage F-18 design and the F-18E/F that brought about the entirely new undesirable behavior? Checking my notes from the aerodynamicist’s lecture I mentioned in Part 2, I find a pretty plausible explanation: ‘Better Idea Creep.’
Some ‘Better Ideas’, in the End… Aren’t
Initially, the F-18E/F was to be a stopgap (for the A-12 and/or later, the JSF). The initial concept was to simply scale up the wing and control surfaces about 25%, put fuselage ‘plugs’ in to increase fuel capacity and put bigger engines in the stretched fuselage to power it all.
The first ‘better idea’ came from the structure guys. They’d felt the Heritage F-18 wings weren’t quite rigid enough and wanted a less flexible wing. They sold the idea of increasing the wing thickness to improve stiffness and allow a lighter structural weight ratio as well as adding more fuel volume. The next ‘better idea’ came from the “systems guys” who sold the idea of reducing the proportions of the leading edge flap chord, which meant lower hinge moments, which allowed reuse of the Heritage Hornet actuator designs and save money. That move also meant even more fuel could be carried in the wings.
“We ‘Aeros’ put twist and camber in a wing for very good reasons. We don’t do it to irritate Structural and/or Manufacturing Engineers. It’s a ‘bonus’, but it’s not why we do it.” (To paraphrase a certain Aerodynamicist)
Early F-18E/F Modeling showed that simply scaling up the F-18C/D wing, with the original twist and camber, would increase supersonic drag and threaten the ability to beat the time maximum time requirement for dashing from subsonic to supersonic. This brought about the next ‘better idea’: ‘straighten’ the wing to reduce supersonic drag. Straightening the wing was seen as beneficial in lowering manufacturing costs as well.

The next ‘better idea’, theoretically to improve resultant high lift performance, was to put a leading edge ‘snag’ at the outer third of the wing that would generate a vortex. This move was puzzling. As one of my ‘Aero’ lecturers noted: it didn’t work on the F-18A, so it was taken out of the C model. What made the designers think it was a good idea to bring it back? My lecturer observed that it was probably due as much to the design culture at Boeing née McDonnell Douglas St Louis, which has seemed to favor using leading edge ‘snags’ for decades (most prominently the F-4 Phantom).
The F-18E/F designers then also modified the LEX, but that was believed to more likely have been done to aid in eliminating the ‘alpha hang-up’ mode and increase ability to point the nose down in such an event. I should also add here that the E/F’s wing drop ‘fix’ of making the wing fold cover ‘porous’ is believed to have a supersonic drag penalty greater than there would have been if the designers had left the twist and camber in place.
All the successive changes didn’t trigger alarms in (the right) people’s minds that maybe the F-18E/F would no longer be quite as simple a derivative as it was first proposed. The F-18E/F did not have to go through nearly as many ‘wickets’ as a new-start program (GAO,1994). The wind-tunnel and computer simulation effort was not as thorough as a clean-sheet design (such as the F-35) would have executed prior to design freeze and manufacture. Only AFTER the F-18E/F was actually flying was the scope of the problem revealed. Not that a full wind tunnel and simulation would have helped. The Abrupt Wing Stall (AWS) program instituted after the F-18E/F wing drop made its self known required increased computing power and more detailed wind tunnel data to adequately examine the phenomenon.
What the wing design changes DID produce was an airfoil system that had a very steep pressure gradient with a propensity to abruptly (there’s that word again) move forward with massive airflow separation at only a moderate angle-of attack in the high subsonic speed range. Observe the flow patterns resulting from taking a baseline F-18C wing, and adding F-18E/F design features:
The ‘red’ colors highlight the position, volume and amplitude of areas with REVERSE airflow and stall. What this phenomenon looks like on an actual F-18E is illustrated below in these snapshots taken from a video (Hall & Woodson):